[1]胡忠伟,盛志广,刘杰,等.余隙无级调节系统在汽油加氢活塞压缩机上的应用[J].石油化工设备,2025,54(02):82-87.[doi:10.3969/j.issn.1000-7466.2025.02.014]
 HU Zhong-wei,SHENG Zhi-guang,LIU Jie,et al.Application of Continuously Variable Clearance Adjustment System in Gasoline-Hydrogen Piston Compressors[J].Petro-Chemical Equipment,2025,54(02):82-87.[doi:10.3969/j.issn.1000-7466.2025.02.014]
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余隙无级调节系统在汽油加氢活塞压缩机上的应用()
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石油化工设备[ISSN:1000-7466/CN:62-1078/TQ]

卷:
54
期数:
2025年02期
页码:
82-87
栏目:
技术应用
出版日期:
2025-03-25

文章信息/Info

Title:
Application of Continuously Variable Clearance Adjustment System in Gasoline-Hydrogen Piston Compressors
文章编号:
1000-7466(2025)02-0082-06
作者:
胡忠伟1盛志广1刘杰1顾姝靓2
1.东明中油燃料石化有限公司,山东 东明 274500; 2.山东易阳石化节能装备有限公司,山东 济南 250101
Author(s):
HU Zhong-wei1 SHENG Zhi-guang1 LIU Jie1 GU Shu-liang2
1.Dongming Zhongyou Fuel and Chemical Co. Ltd., Dongming 274500, China; 2.Shandong Yiyang Petrochemical Energy-Saving Equipment Co. Ltd., Jinan 250101, China
关键词:
压缩机余隙无级调节汽油加氢节能降碳
Keywords:
compressorclearance volume step-less regulation gasoline hydrogenation energy saving and carbon reduction
分类号:
TQ051.21
DOI:
10.3969/j.issn.1000-7466.2025.02.014
文献标志码:
A
摘要:
节能降碳是积极稳妥推进碳达峰碳中和、全面推进美丽中国建设和促进经济社会发展全面绿色转型的重要举措。实践证明,余隙无级调节气量节能技术产品成熟、运行稳定可靠,节能降碳效果显著,非常适用于炼油化工领域往复活塞压缩机的节能改造,是践行国务院《2024—2025年节能降碳行动方案》的友好型节能技术。某公司第六联合车间于2023-10利用余隙无级调节气量节能技术对汽油加氢一段K3201B和二段K3601B循环氢活塞压缩机进行了余隙节能改造,改造后,2台压缩机每日节约电量合计为7 210 kW·h,年节约电量合计为252.4万 kW·h,年节约电费151.4万元,年节约能量合计为832.92 t标准煤,年减排二氧化碳合计为2 198.9 t。该节能技术具有良好的经济效益和社会效益,值得大力推广和应用。
Abstract:
The implementation of energy conservation and carbon reduction measures is a crucial step in achieving the goals of Carbon Peak and Carbon Neutral, and in promoting a comprehensive green transformation of economic and social development. The energy-saving technology of step-less capacity regulation with variable clearance volume is highly suitable for reciprocating piston compressors in the field of refining and the chemical industry. The technical products offer numerous advantages, including stable and reliable operation, notable energy savings and carbon reduction. In the sixth joint workshop of a company, the energy-saving transformation technology for circulating hydrogen piston compressors K3201B and K3601B, which are used in the first and second stages of gasoline hydrogenation, respectively, was carried out in October 2023. The results of the transformation demonstrate the following: the total daily power saving of the two compressors is 7 210 kW·h, the total annual power saving is 2.524 million kW·h, the annual electricity saving cost is 1.514 million RMB, the total annual energy saving is 832.92 ton of standard coal equivalent and the total annual carbon dioxide emission reduction is 2 198.9 t. Therefore, this energy-saving technology offers significant economic and social benefits and merits vigorous promotion and application.

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备注/Memo

备注/Memo:
收稿日期: 2024-12-10
作者简介:胡忠伟(1982-),男,山东东明人,工程师,学士,现主要从事炼油化工生产车间的管理工作。E-mail:18905306058@163.com。
通信作者:顾姝靓(1996-),女,山东济南人,硕士,现主要从事往复活塞压缩机节能技术的研发等工作。E-mail:479118868@qq.com。
更新日期/Last Update: 2025-03-25